Compressed Air System Upgrade Results In Substantial Energy Savings
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Total Pages | : 0 |
Release | : 2002 |
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This case study highlights a compressed air system upgrade at BWX Technologies manufacturing plant in Lynchburg, Virginia, which replaced antiquated compressors and dryers and implemented an improved control strategy, resulting in improved energy efficiency and savings in energy and maintenance costs.
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Total Pages | : 4 |
Release | : 2002 |
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This case study highlights a compressed air system upgrade at BWX Technologies manufacturing plant in Lynchburg, Virginia, which replaced antiquated compressors and dryers and implemented an improved control strategy, resulting in improved energy efficiency and savings in energy and maintenance costs.
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Publisher | : U.S. Department of Energy |
Total Pages | : 128 |
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Genre | : Technology & Engineering |
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Release | : 2010 |
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In 1996, U.S. Steel completed a project in which the main compressed air system at their Edgar Thomson plant in Braddock, Pennsylvania was overhauled.
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Total Pages | : 20 |
Release | : 1997 |
Genre | : Air-compressors |
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Compressed air is a versatile medium used in industry for performing a variety of tasks. It is, however, not cheap. By the time it arrives at its point of use, the energy consumption and costs of the system are already high. Therefore, it is worthwhile investigating ways of making compressed air systems more efficient. This brochure describes how a thorough investigation of a compressed air system can highlight many areas for saving energy. Improvements can be made by optimising the compressed air cycle itself and the compressed air usage, or by such obvious good housekeeping measures as plugging leaks.
Author | : E. M. Talbott |
Publisher | : |
Total Pages | : 216 |
Release | : 1986 |
Genre | : Technology & Engineering |
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Total Pages | : 5 |
Release | : 2001 |
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This case study is one in a series on industrial firms who are implementing energy efficient technologies and system improvements into their manufacturing processes. This case study documents the activities, savings, and lessons learned on the Caterpillar's Pontiac Plant project.
Author | : Great Britain. Energy Efficiency Office |
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Release | : 1993 |
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Total Pages | : 6 |
Release | : 2002 |
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This case study highlights International Truck and Engine Corporation's optimization project on the compressed air system that serves its foundry, Indianapolis Casting Corporation. Due to the project's implementation, the system's efficiency was greatly improved, allowing the foundry to operate with less compressor capacity, which resulted in reduced energy consumption, significant maintenance savings, and more reliable production.
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Total Pages | : |
Release | : 2001 |
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This case study is one in a series on industrial firms who are implementing energy efficient technologies and system improvements into their manufacturing processes. This case study documents the activities, savings, and lessons learned on the Caterpillar's Pontiac Plant project.